Thursday, October 8, 2009

Leo's First Run

Well, he lucked out on his first run, only found half of the corners and got stuck in every one of them *chuckles*. Otherwise, it was a great and informative maiden run. Especially, considering that the only sensors he has right now are his bumper switches. The next project will be to adding some range finders to him so he can hopefully avoid obstacles altogether. Though adding another 7805 FET would probably be a good idea if I want to add some juice to his motors. I need to get more rechargeable batteries as well, it seems that most of mine are dead and I do mean dead as in won't take a charge dead.

I'll try to upload the video of Leo's first run tomorrow. The lighting is bad and there is no sound, but it's a cool video still.

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